United Airlines Flight 232

United Airlines Flight 232
United Airlines Flight 232

N1819U on its final descent, with visible damage on the horizontal stabilizer and fuselage tail cone
Accident summary
Date July 19, 1989 (1989-07-19)
Type Engine failure, hydraulic system destruction, loss of flight controls
Site Sioux City, Iowa,
United States
Passengers 285[1]
Crew 11[1]
Injuries 172[1]
Fatalities 111[note 1][1]
Survivors 185[1]
Aircraft type McDonnell Douglas DC-10-10
Operator United Airlines
Tail number N1819U
Flight origin Stapleton International Airport
Stopover O'Hare International Airport
Destination Philadelphia International Airport

United Airlines Flight 232 was a scheduled flight from Stapleton International Airport in Denver, Colorado, to O'Hare International Airport in Chicago, with continuing service to Philadelphia International Airport. On July 19, 1989, the DC-10 (Registration N1819U) operating the route crash-landed in Sioux City, Iowa, after suffering catastrophic failure of its tail-mounted engine, which led to the loss of all flight controls. 111 people died in the accident while 185 survived.[note 1] Despite the deaths, the accident is considered a prime example of successful crew resource management due to the manner in which the flight crew handled the emergency, and the high number of survivors considering that the airplane was landed without conventional control. The flight crew became well-known as a result of their actions that day, in particular the captain, Alfred C. Haynes, and a DC-10 instructor on board who offered his assistance, Dennis E. Fitch.

The manner in which the engine failed resulted in high-speed shrapnel being hurled from the engine; this shrapnel penetrated the hydraulic lines of all three independent hydraulic systems on board the aircraft, which rapidly lost their hydraulic fluid. As the flight controls on the DC-10 are hydraulically powered, the flight crew lost their ability to operate nearly all of them. Despite these losses, the crew were able to attain and then maintain limited control by using the only systems still workable: the two remaining engines. By utilizing each engine independently, the crew made rough steering adjustments, and by using the engines together they were able to roughly adjust altitude. The crew guided the crippled jet to Sioux Gateway Airport and lined it up for landing on one of the runways. Without flight controls, they were unable to slow down for landing, and were forced to attempt landing at much too high a speed and rate of descent. On touchdown, the aircraft broke apart, caught fire, and rolled over. The largest section came to rest in a cornfield next to the runway. Despite the ferocity of the accident, approximately two-thirds of those on board survived due to multiple factors. The cause of the engine failure was traced back to a manufacturing defect in the fan disk, which had microscopic cracks due to impurities. The cracking was present during maintenance inspections and should have been detected by maintenance personnel, revealing shortcomings in the maintenance processes.

The accident had a strong impact on the industry. DC-10s were modified to prevent catastrophic loss of hydraulic fluid should a similar failure occur again. These modifications were also included in the DC-10's direct successor, the MD-11. Research has been conducted to see if computers might be able to control aircraft using the engines alone, improving on what humans can do unaided. The accident is cited as an example of why "lap infants"—children without a seat of their own—should have their own seat and be properly restrained on all flights. This campaign has been led by United 232's chief flight attendant, one of the notable survivors of the accident. Several other notable people survived, and the news photography in the direct aftermath led to an iconic image being produced; that image was transformed into sculpture and now serves as flight 232's memorial.

Contents

Chronology of the flight

Radar plot of the plane's flight path, from the NTSB report
Damage to the rear of the plane, from the NTSB report
Locations of passengers indicated by lack of injury, severity of injury, and reason of death from the NTSB report

The flight took off at 14:09 (CDT) from Stapleton International Airport, Denver, Colorado, bound for O'Hare International Airport in Chicago, with ongoing service to Philadelphia International Airport. At 15:16, while the plane was in a shallow right turn at 37,000 feet, the fan disk of its tail-mounted General Electric CF6-6 engine failed and disintegrated. The debris from the failed disk was not contained by the engine's nacelle, a housing that protects the engine. Pieces of the structure penetrated the aircraft tail section in numerous places, including the horizontal stabilizer. This shrapnel punctured the lines of all three hydraulic systems, allowing the fluid to rapidly drain away.[2]

Captain Alfred C. Haynes and his flight crew, First Officer William Records, copilot, and Second Officer Dudley Dvorak, flight engineer, felt a jolt go through the aircraft. Warning lights illuminated which indicated that the autopilot had disengaged and the tail-mounted number two engine was malfunctioning. Captain Haynes watched First Officer Records place his hands on the flight controls in response to the autopilot disconnecting and therefore focused his attention on the malfunctioning engine. Second Officer Dvorak obtained the engine failure checklist and read the first item: throttle power must be reduced to idle. Haynes was unable to move the throttle; the linkage had been jammed as a result of the engine failure.[2] The second item called for the fuel supply lever to be pulled to shutoff, but it would not move either. At this point, at Dvorak's suggestion, the firewall shutoff valve was actuated, and the fuel flow to the engine was shut off.[2] This part of the emergency took 14 seconds.[2]

Meanwhile, Records noticed that the airliner was off course, and moved his control column to correct this, but the plane did not respond.[1] Records reported to Captain Haynes that he could not control the airplane. Haynes, having just shut off the fuel supply to the malfunctioning engine, looked at Records and was surprised by what he saw: Records had the control column turned all the way to the left, commanding maximum left aileron, and pulled all the way back, commanding maximum up elevator.[2] These inputs would never be utilized simultaneously in normal flight. What was more, despite these inputs, which command a roll to the left and the aircraft's nose to rise, the aircraft was instead banking to the right with the nose dropping.[2] Haynes took the flight controls and attempted to level the aircraft with his own control column.[2] When this was ineffective, both Haynes and Records utilized their control columns at the same time in an attempt to recover from the steepening bank. The aircraft still did not respond. Out of options, and in danger of the aircraft rolling into a completely inverted position (an unrecoverable situation which would result in a crash), the crew took the throttle for the left wing mounted number 1 engine and reduced the power to idle, while also taking the throttle for the right wing mounted number 3 engine and commanding maximum power. The resulting differential thrust (no power on the left side and maximum power on the right side) caused the airplane to slowly level out.[2]

With the imminent danger over for the time being, the crew began to diagnose the situation on the flight deck. Dvorak discovered that the pressure gauges and quantity gauges on his instrument panel for the three hydraulic systems were registering zero, and reported this to Haynes.[2] The three hydraulic systems were separate; a single event in one system would not disable the other systems, but lines for all three systems shared the same 10-inch-wide (250 mm) route through the tail where the engine debris had penetrated. There was no additional backup system. The flight crew quickly realized that the initial failure had left all hydraulic systems, and therefore all control surfaces, inoperative.[1] The crew called United Airlines maintenance base using one of their radios, but as a total loss of hydraulics on the DC-10 was considered "virtually impossible", there were no procedures or guidelines for dealing with such an event.[1]

Due to the damage in the tail, the plane had a continual tendency to turn right, and without flight controls it was difficult to maintain a stable course. The plane began to slowly oscillate vertically in a phugoid cycle, which is characteristic of planes in which control surface command is lost. With each iteration of the cycle the aircraft lost approximately 1,500 feet (460 m) of altitude. Dennis E. Fitch, an off-duty United Airlines DC-10 flight instructor, was seated in the first class section and, noticing the crew were having trouble controlling the airplane, offered his assistance to the flight attendants. Upon being informed that there was a DC-10 instructor on board, Haynes immediately invited him to the cockpit, hoping his instructional knowledge of the aircraft would help them regain control.[2] Upon entering the cockpit and looking at the hydraulic gauges, Fitch determined that the situation was beyond anything he had ever faced.[2] The flight crew, while using the engines to control the airplane, were also still trying to fly the airplane using their control columns. Haynes asked Fitch to go into the passenger cabin and see if their control inputs were having any effect on the ailerons.[2] Fitch reported back that the ailerons were not moving at all. Despite this news, the crew would continue trying to fly the airplane with their control columns for the remainder of the flight, hopeful that it was at least having some effect. Fitch, his first task concluded, asked how he might be of further assistance. Haynes, still trying to fly the airplane with his control column while simultaneously working the throttles, asked Fitch to work the throttles instead. With one throttle in each hand, Fitch was able to mitigate the phugoid cycle and make rough steering adjustments.

Air traffic control (ATC) was contacted and an emergency landing at nearby Sioux Gateway Airport was organized.

Haynes kept his sense of humor during the emergency, as recorded on the plane's cockpit voice recorder (CVR):

Fitch: I'll tell you what, we'll have a beer when this is all done."[3]
Haynes: Well I don't drink, but I'll sure as hell have one."[3]

and later:

Sioux City Approach: United Two Thirty-Two Heavy, the wind's currently three six zero at one one; three sixty at eleven. You're cleared to land on any runway.[3]
Haynes: [laughter] Roger. [laughter] You want to be particular and make it a runway, huh?[3] (Haynes was alluding to the extreme difficulty in controlling the aircraft and their extremely low chances of making it to the airport at all.)[4]

A more serious remark often quoted from Haynes was made when ATC asked the crew to make a left turn to keep them clear of the city:

Haynes: Whatever you do, keep us away from the city.[5]

Haynes later noted that "We were too busy [to be scared]. You must maintain your composure in the airplane or you will die. You learn that from your first day flying."[6]

As the crew began to prepare for arrival at Sioux City, they questioned whether they should deploy the landing gear or belly-land the aircraft with the gear retracted. They decided that having the landing gear down would provide some shock absorption on impact.[7] However, the complete hydraulic failure left the landing gear lowering mechanism inoperative. Two options were available to the flight crew. The DC-10 is designed such that if hydraulic pressure to the landing gear is lost, it will fall down slightly and rest on the landing gear doors. Placing the regular landing gear handle into the down position will unlock the doors mechanically, and the doors and landing gear will then fall down into place and lock due to gravity.[7] An alternate system is also available where the gear will fall into position by pulling a lever in the cockpit floor.[8] This lever has the added benefit of unlocking the outboard ailerons, which are not used in high-speed flight and are locked in a neutral position.[7] The crew hoped that there might be some trapped hydraulic fluid in the outboard ailerons and that they might regain some use of flight controls by unlocking them. They elected to extend the gear with the alternate system.[7] Although the gear deployed successfully, there was no change in the controllability of the aircraft.[1]

Landing was originally planned on the 9,000-foot (2,700 m) Runway 31. Difficulties in controlling the aircraft made lining up almost impossible. While dumping excess fuel, the plane executed a series of mostly right-hand turns (it was easier to turn the plane in this direction) with the intention of lining up with Runway 31. When they came out they were instead lined up with the shorter (6,600 ft) Runway 22, and had little capacity to maneuver.[1] Fire trucks had been placed on Runway 22,[2] anticipating a landing on Runway 31, so all the vehicles were quickly moved out of the way before the plane touched down.

Fitch continued to control the aircraft's descent by adjusting engine thrust. With the loss of all hydraulics, the crew were unable to control airspeed independent from sink rate. On final descent, the aircraft was going 240 knots and sinking at 1,850 feet per minute, while a safe landing would require 140 knots and 300 feet per minute. Fitch needed a seat for landing; Dvorak offered up his own, as it could be moved to a position behind the throttles.[1] Dvorak sat in the cockpit's jump seat for landing. Unfortunately, right before touchdown, the aircraft began a downward phugoid and veered right. The flight crew had no time to react. The tip of the right wing hit the runway first, spilling fuel, which ignited immediately. The tail section broke off from the force of the impact, and the rest of the aircraft bounced several times, shedding the landing gear and engine nacelles and breaking the fuselage into several main pieces. On the final impact the right wing was sheared off and the main part of the aircraft skidded sideways, rolled over on to its back, and slid to a stop upside-down in a corn field to the right of Runway 22. Witnesses reported that the aircraft cartwheeled, but the investigation did not confirm this.[1] News reports that the aircraft cartwheeled were due to misinterpretation of the video of the crash that showed the flaming right wing tumbling end-over-end and the intact left wing, still attached to the fuselage, rolling up and over as the fuselage flipped over.

The plane landed askew, causing the explosion and fire seen in this still from local news station video.

Of the 296 people on board, 111 died in the crash.[note 1] Most were killed by injuries sustained in the multiple impacts, but 35 people in the middle fuselage section directly above the fuel tanks died from smoke inhalation in the post-crash fire. Of those, 24 had no traumatic blunt-force injuries. The majority of the 185 survivors were seated behind first class and ahead of the wings.[5] Many passengers were able to walk out through the ruptures to the structure, and in many cases got lost in the high field of corn adjacent to the runway until rescue workers arrived on the scene and escorted them to safety.

Of all of the passengers:[1]

  • 35 died due to smoke inhalation (none were in first class)
  • 76 died for reasons other than smoke inhalation (17 were in first class)
  • 47 were seriously injured (8 were in first class)
  • 125 had minor injuries (1 was in first class)
  • 13 had no injuries (None were in first class)

The passengers who died for reasons other than smoke inhalation were seated in rows 1–4, 24–25, and 28–38. Passengers who died due to smoke inhalation were seated in rows 14, 16, and 22–30. A person assigned to 20H moved to an unknown seat and died due to smoke inhalation.

One crash survivor died 31 days after the accident; in accordance with official rules, the NTSB classified his injuries as "serious."[1]

Fifty-two children, including four "lap children" without their own seats, were on board the flight due to the United Airlines "Children's Day" promotion. Eleven children, including one lap child, died.[9] Many of the children had traveled alone.[10]

Rescuers initially ignored the cockpit, as it had been compressed in the crash to approximately waist high and was completely unrecognizable. It was not until 35 minutes after the crash that rescuers discovered that the debris was the cockpit and that the four pilots were still alive inside. All four would recover from their injuries and return to work: Haynes, Records, and Dvorak would return in three months, while Fitch, more seriously injured than the others, would return in 11 months.[2]

Investigation

Part of the DC-10's fuselage after the crash

National Transportation Safety Board officials were on scene within hours of the accident. As the investigation unfolded, it became apparent that the entire fan disk and blade assembly from engine number 2, a component approximately 8 feet (2.4 m) in diameter and made of titanium alloy, was missing from the accident scene.[1] Despite an extensive search in the weeks following the crash, the fan disk could not be located. Realizing that finding the fan disk was potentially the key to understanding the reasons for the engine failure, the engine's manufacturer, GE, offered a $50,000 reward to whoever could locate the disk, and $1,000 for each fan blade.[11] On October 10, 1989, three months after the crash, a farmer harvesting corn near Alta, Iowa felt resistance on her combine, and after getting out to see what was causing it, discovered most of the fan disk with a number of blades still attached partially buried in her cornfield.[11] The rest of the fan disk would also be located later in the harvest.

Examination of the fan disk would indeed solve the mystery. Investigators discovered an impurity and fatigue crack in the disk, and traced this back to the Alcoa foundry from which the engine part originated. The investigation showed there was a defect in the elimination of gaseous anomalies during the purifying of the titanium disk ingot. An excess amount of nitrogen was in the material, causing a 'hard alpha inclusion', which cracked during forging and then fell out during final machining. This formed a cavity with microscopic cracks at the edges. During the engine's normal running cycle, one of these cracks grew slowly each time the engine was powered up and brought to operating temperature, until it grew large enough for the disk to fail structurally.[1] Newer batches used much higher melting temperatures and a "triple vacuum" process to eliminate these impurities.[12]

The subsequent investigation and Airworthiness Directive revealed several other fan disks already in service from the same batch of ingots which had started to exhibit the initial cracking symptoms of part failure.[1]

Cause

The recovered fan disk from the center engine of UAL 232. The fracture is clearly visible.

The investigation, while praising the actions of the flight crew for saving lives, would later attribute the cause of the accident to a failure of United Airlines maintenance processes and personnel to detect an existing fatigue crack.[1] Post-crash analysis of the crack surfaces showed the presence of a penetrating fluorescent dye used to detect cracks during maintenance. The presence of the dye indicated that the crack was present and should have been detected at a prior inspection. The detection failure arose from poor attention to human factors in United Airlines' specification of maintenance processes.[1]

Influence on the industry

Damage to N1819U's three hydraulic systems

The National Transportation Safety Board (NTSB) investigation, after subsequent reconstructions of the accident in flight simulators, deemed that training for such an event involved too many factors to be practical. While some level of control was possible, no precision could be achieved, and a landing under these conditions was stated to be "a highly random event".[1] The NTSB further noted that "under the circumstances the UAL[note 2] flight crew performance was highly commendable and greatly exceeded reasonable expectations."[1]

Because this type of aircraft control is difficult for humans to achieve, some researchers have attempted to integrate this control ability into the computers of fly-by-wire aircraft. Early attempts to add the ability to real airplanes were not very successful; the software was based on experiments conducted in flight simulators where jet engines are usually modeled as "perfect" devices with exactly the same thrust on each engine, a linear relationship between throttle setting and thrust, and instantaneous response to input. Later, computer models were updated to account for these factors, and planes have been successfully flown with this software installed.[13]

Newer aircraft designs such as the MD-11 have incorporated hydraulic fuses to isolate a punctured section and prevent a total loss of hydraulic fluid. Following the UAL 232 accident, such fuses were installed in the number 3 hydraulic system in the area below the number 2 engine on all DC-10 aircraft to ensure sufficient control capability remained if all three hydraulic system lines should be damaged in the tail area in the future.[5] Although elevator and rudder control would be lost, the aircrew would still be able to control the aircraft's pitch (up and down) with stabilizer trim, and would be able to control roll (left and right) with some of the aircraft's ailerons and spoilers. Although not an ideal situation, the system provides a greater measure of control than was available to the crew of United 232.

It is still possible to lose all three hydraulic systems if serious damage occurs elsewhere, as nearly happened to a cargo airliner in 2002 during takeoff when a main gear tire exploded in the wheel well area. The damage in the left wing area caused total fluid loss from the number 1 and the number 2 hydraulic systems. The number 3 system was dented but not penetrated. DC-10s still have no fuse protection for any of the three hydraulic systems in the event of an exploding main gear tire.[14]

Of the four children deemed too young to have seats of their own ("lap children"), one died from smoke inhalation.[1] The NTSB added a safety recommendation to the FAA on its "List of Most Wanted Safety Improvements" in May 1999 suggesting a requirement for children under 2 to be safely restrained, which was removed in November 2006.[15][16] The accident sparked a campaign led by United Flight 232's senior flight attendant, Jan Brown Lohr, for all children to have seats on aircraft.[17]

The accident has since become a prime example of successful Crew Resource Management.[18] For much of aviation's history, the Captain was considered the final authority, and crews were to respect the Captain's expertise and not question him. This began to change in the 1970s especially after the Tenerife Disaster. Crew Resource Management, while still considering the Captain the final authority, instructs crewmembers to speak up when they detect a problem, and instructs Captains to listen to crewmember concerns. United Airlines instituted a Crew Resource Management class in the early 1980s. The NTSB would later credit this training as valuable toward the success of United 232's crew in handling their emergency.[1] The FAA made Crew Resource Training mandatory in the aftermath of the accident.

Factors contributing to survival

Of the 296 people aboard, 111 were killed in the crash, while 185 survived.[note 1] Captain Haynes later told of three contributing factors regarding the time of day that allowed for a better chance of survival:

  1. The accident occurred during daylight hours;
  2. The accident occurred as a shift change was occurring at both a regional trauma center and a regional burn center in Sioux City, allowing for more medical personnel to treat the injured; and
  3. The accident occurred when the Iowa Air National Guard was on duty at Sioux Gateway Airport, allowing for 285 trained personnel to assist with triage and evacuation of the injured.

"Had any of those things not been there," Haynes said, "I'm sure the fatality rate would have been a lot higher."[19]

As with the Eastern Air Lines Flight 401 crash of a similarly-sized Lockheed L-1011 in 1972, the relatively shallow angle[note 3] of descent likely played a large part in the relatively high survival rate. The National Transportation Safety Board concluded that under the circumstances, "a safe landing was virtually impossible."[1]

Notable survivors

Spencer Bailey, a young survivor, being carried to safety by Lt. Colonel Dennis Nielsen after the crash
  • Spencer Bailey – Subject of a famous photograph showing Lt. Colonel Dennis Nielsen carrying the three-year-old survivor to safety.[20] His brother Brandon also survived the crash, but their mother, Francie, did not.[20] A statue in part of Sioux City's riverfront development is based on the picture.[20] The 1994 memorial commemorates the rescue efforts by the Sioux City community following the crash, and features contemplative areas and a tree-lined approach with plaques describing the accident.[20] Bailey works as an editor and journalist in New York City.[21]
  • Jerry Schemmel – Radio announcer for the Colorado Rockies, Denver's Major League Baseball team, and a former radio announcer for the Denver Nuggets, Denver's National Basketball Association basketball team. He wrote a book about United Airlines Flight 232 titled Chosen to Live, and was credited with saving the life of a child in the crash.[22]
  • Michael R. Matz – Trainer of the 2006 Kentucky Derby favorite and winner Barbaro. He was credited with saving the lives of four children in the crash, three of whom were in the same family. Matz competed for the US in equestrian show jumping in several Summer Olympics, including 1976, 1992, and 1996. He won silver in the team show jumping event at the 1996 games.[23]
  • Alfred C. Haynes – The Captain of United Airlines flight 232. His actions, along with the actions of the entire flight crew, are partially credited for saving the lives of the survivors.[1] He returned to flying after recovering from his injuries and would continue to fly DC-10s as captain until reaching mandatory retirement age in 1991. Several rescuers, crew members, and passengers from flight 232 flew with Haynes on his final flight.[24] Haynes became a public speaker soon after the accident, giving speeches about what happened aboard flight 232. He continues these to the present day, and credits this work with helping his own healing process.[25]
  • Dennis E. Fitch – A DC-10 pilot and instructor, he helped Captain Al Haynes fly United Airlines Flight 232. "For the 30 minutes I was up there," Fitch said, "I was the most alive I've ever been. That is the only way I can describe it to you."[19]
  • Pete Wernick – Prominent banjo player with the Hot Rize bluegrass band and instructor, he was on his way to a festival in the Albany, New York area. Wernick walked away from the crash with his young son, and along with his wife, they took a later flight to go to the festival. He gave his personal account of the day's events in the song "A Day in '89 (You Never Know)". Wernick has yet to release a recording of the song, but has published the lyrics on his website.[26]
  • Jan Brown Lohr – United 232's Senior Flight Attendant. She was forced by regulation to ask parents with "lap children" aboard flight 232 to place their children on the cabin floor during the flight's final moments before impact. One of four children died from smoke inhalation. The deceased child's grief-stricken mother confronted Lohr at the crash scene. Since then, Lohr has tirelessly lobbied in Washington D.C. to promote the safety of children on all civilian aircraft and airlines, asking that federal regulations require all children to have a seat belt on every flight.[17]

In popular culture

  • The accident was the subject of the 1992 television movie, Crash Landing: The Rescue of Flight 232,[27] (also known as A Thousand Heroes).
  • It was featured in an episode of Seconds From Disaster on the National Geographic Channel and MSNBC Investigates on the MSNBC news channel.
  • It was one of the inspirations for the crash in Peter Weir's 1993 film version of Fearless, adapted from a novel by Rafael Yglesias.
  • The DC-10 crash in the 1991 Dean Koontz novel Cold Fire is based on this accident.
  • The cockpit voice recording of the accident became part of the script of a play called Charlie Victor Romeo.
  • Dennis Fitch described his experiences in Errol Morris' television show First Person.[28]
  • Martha Conant told her story of survival to her daughter-in-law, Brittany Conant, on "Storycorps" during NPR's Morning Edition of January 11, 2008.[29]
  • The History Channel distributed a documentary named Shockwave; a portion of Episode 7 (originally aired January 25, 2008) detailed the events of the crash.
  • The episode "A Wing and a Prayer" of The Black Box featured the accident.
  • The Biography Channel series I Survived... explained in detail the events of the crash through passenger Jerry, flight attendant Jan Brown Lohr, and pilot Alfred Haynes.
  • The band Leæther Strip released a song called Crash Flight 232, which mentions the crash throughout the entire song.

Similar accidents

The odds against all three hydraulic systems failing simultaneously had previously been calculated as high as a billion to one.[30] Yet, similar flight control failures have occurred:

  • In 1971 a Pan American 747 struck approach light structures for the reciprocal runway as it lifted off the runway at San Francisco Airport. Major damage to the belly and landing gear resulted, which caused the loss of hydraulic fluid from three of its four flight control systems. The fluid which remained in the fourth system gave the captain very limited control of some of the spoilers, ailerons, and one inboard elevator. That was sufficient to circle the plane while fuel was dumped and then to make a hard landing. There were no fatalities, but there were some injuries.[31]
  • In 1981, Eastern Airlines Flight 935, operated by a Lockheed L-1011 suffered a similar kind of massive failure of its tail mounted number two engine. The shrapnel from that engine inflicted damage on all four of its hydraulic systems, which were also close together in the tail structure. Fluid was lost in three of the four systems. While the fourth hydraulic system was impacted with shrapnel too, it was not punctured. The hydraulic pressure remaining in that fourth system enabled the captain to land the plane safely with some limited use of the outboard spoilers, the inboard ailerons, and the horizontal stabilizer, plus differential engine power of the remaining two engines. There were no injuries.[32]
  • In 1985 Japan Airlines flight 123, a Boeing 747, suffered a rupture of the pressure bulkhead in its tail section. The damage was extensive and caused the loss of fluid in all four of its hydraulic control systems. The pilots were able to keep the plane airborne for almost 30 minutes using differential engine power, but eventually control was lost, and the plane crashed in mountainous terrain. There were only 4 survivors among the 524 on board. This accident is the deadliest single-aircraft accident in history.[33]
  • In 1994, RA85656, a Tupolev Tu-154 operating as Baikal Airlines Flight 130, crashed near Irkutsk shortly after departing from Irkutsk Airport, Russia. Damage to the starter caused a fire in engine number two (located in the rear of fuselage). High temperatures during the fire destroyed the tanks and pipes of all three hydraulic systems. The crew lost control of the aircraft. The unmanageable plane, at a speed of 275 knots, hit the ground at a dairy farm and burned. All passengers and crew, as well as a dairyman on the ground, died.[34]
  • In 2003, OO-DLL, a DHL Airbus A300 was struck by a surface-to-air missile shortly after departing from Baghdad International Airport, Iraq. The missile struck the port side wing, rupturing a fuel tank and causing the loss of all three hydraulic systems. With the flight controls disabled, the crew was able to use differential thrust to execute a safe landing at Baghdad. This is the first and only documented time anyone has managed to land a transport aircraft safely without working flight controls.[35]

The disintegration of a turbine disc, leading to loss of control, was a direct cause of two major aircraft disasters in Poland:

  • On March 14, 1980, LOT Polish Airlines Flight 007, an Ilyushin Il-62, attempted a go-around when the crew experienced troubles with a gear indicator. When thrust was applied, low pressure turbine disc in engine number 2 disintegrated because of material fatigue; parts of the disc damaged engines number 1 and 3 and severed control pushers for both horizontal and vertical stabilizers. After 26 seconds of uncontrolled descent, the aircraft crashed, killing all 87 people on board.[36]
  • On May 9, 1987, improperly assembled bearings in engine number 2 on LOT Polish Airlines Flight 5055 overheated and exploded during cruise over Lipniki village, causing the shaft to break in two; this caused the low pressure turbine disc to spin to enormous speeds and disintegrate, damaging engine number 1 and cutting the control pushers. The crew managed to return to Warsaw, using nothing but trim tabs to control the Il-62M, but on the final approach, the trim controlling links burned and the crew completely lost control over the aircraft. Soon after, it crashed on the outskirts of Warsaw; all 183 on board perished. Had the plane stayed airborne for 40 seconds more, it would have been able to reach the runway.[37]

See also

Notes

  1. ^ a b c d One passenger died 31 days after the accident; in accordance with NTSB regulations, he is classified as a survivor with "serious" injuries.
  2. ^ UAL is the three-letter designator code for United Airlines.
  3. ^ Angle of descent and Rate of descent are two different things. The aircraft approached at a high rate of descent but a shallow angle.

References

  1. ^ a b c d e f g h i j k l m n o p q r s t u v w x y "NTSB/AAR-SO/06". NTSB. http://www.airdisaster.com/reports/ntsb/AAR90-06.pdf. Retrieved 2011-03-15. 
  2. ^ a b c d e f g h i j k l m n Haynes, Al. "Special report". Airdisaster.com. http://www.airdisaster.com/special/special-ua232.shtml. Retrieved 2006-09-15. 
  3. ^ a b c d "Aviation Safety Network CVR/FDR: United Airlines DC-10-10 – 19 JUL 1989". Aviation Safety Network. http://www.tailstrike.com/190789.pdf. Retrieved 25 March 2011. 
  4. ^ "30 minutes that changed everything". CBS News. 1998-08-20. http://www.cbsnews.com/stories/1998/08/20/48hours/main16349.shtml. Retrieved 2006-12-05. 
  5. ^ a b c Macarthur Job (1996). Air Disaster Volume 2, Aerospace Publications, ISBN 1-875671-19-6: pp.186–202
  6. ^ Gates, Dominic (2009-07-19). "20 years ago, pilot's heroic efforts saved 185 people as plane crashed". Seattle Times. http://seattletimes.nwsource.com/html/localnews/2009496792_haynes19m.html. Retrieved 2009-07-19. 
  7. ^ a b c d Haynes, Al. "The Crash of United Flight 232". http://clear-prop.org/aviation/haynes.html. Retrieved 16 March 2011. 
  8. ^ "DC-10 Flight Crew Operating Manual". http://www.scribd.com/doc/32605793/McDonnell-Douglas-DC-10-40-Landing-Gear. Retrieved 16 March 2011. 
  9. ^ United Airlines Flight 232 episode, Seconds From Disaster
  10. ^ "The Crash of United Flight 232 by Capt. Al Haynes". Clear-prop.org. http://www.clear-prop.org/aviation/haynes.html. Retrieved 2011-03-15. 
  11. ^ a b "Key Piece of Doomed DC-10 Found in Field". Los Angeles Times. 1989-10-12. http://articles.latimes.com/1989-10-12/news/mn-304_1_fan-blades. Retrieved 2011-03-15. 
  12. ^ Thomas, Malcolm. "Titanium in Aero Engines, Trends & Developments". Rolls Royce. http://www.specialmetalsforum.com/uploads/docs/1196332700M%20Thomas%20RR.%20presentation.pdf. Retrieved 10 April 2011. 
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External links

Coordinates: 42°24′29″N 96°23′02″W / 42.40806°N 96.38389°W / 42.40806; -96.38389


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