- 1997 Aisin fire
The 1997 Aisin fire was a
fire which shut down one of the production facilities of theToyota -subsidiary Aisin Seiki Co. onFebruary 1 1997 cite web | title=How Toyota Recovered From A Major Fire in Less Than a Week | work=Mirror of Wall Street Journal article | url=http://www.rbbi.com/company/toyota/fire.htm | date=May 8 1997 | accessdate=2006-06-19] , a Saturday. The event was notable as the factory was the main supplier of a motor part for Toyota cars. Due to the just in time stock keeping philosophy of the Toyota Production System (TPS), Toyota's car factories reportedly only kept four-hour stocks of the part . However the event also provided an example of successful business relationships between Toyota and its suppliers, allowing the company to quickly manufacture replacement parts and limit the halt in production of its cars, so minimizing the losses from this event.The fire
The fire started before dawn on February 1 1997 at Aisin Seiki Co.'s Factory No. 1 in
Kariya ,Japan . The cause of the fire was reportedly unknown . The factory producedbrake fluid "proportioning valves " ("P-valves") which help prevent skidding by controlling the pressure on rear brakes, and are used in the braking system of all Toyota vehicles [cite journal
author = Toshihiro Nishiguchi and Alexandre Beaudet
year = 1998
month = Fall
title = The Toyota Group and the Aisin Fire
journal = MIT Sloan Management Review
volume = 40
issue = 1
pages = 49–59
url = http://sloanreview.mit.edu/smr/issue/1998/fall/4/
accessdate = 2006-06-19 ] . 99% of Toyota's P-valves were made at this plant, withNisshin Kogyo Co. producing the remaining 1% . With the factory out of production, it was estimated that Toyota would have to halt car production for weeks. The economic impact of this would have been huge for Toyota, the local economy and for Japan. It was estimated that each day Toyota production was halted would lead to a 0.1% decrease in Japan's industrial output . However Toyota managed to get production restarted within 5 days .Recovery
Aisin, along with Toyota, set up a crisis room to deal with the problem of manufacturing new P-valves. The production of P-valves was complicated, and required specialised tools. Furthermore, different varieties of P-valves were in production. Toyota managed to get many of its suppliers to bring in additional engineers, and work overtime shifts, to help build machines to produce P-valves, as well as increase production of the components. Some of Toyota's suppliers, and their subcontractors, were persuaded to give priority to the production of P-valves. Even a sewing machine manufacturer was persuaded to help provide valves for Toyota. The first usable valves were delivered to Toyota on the Wednesday (February 5) following the fire, allowing production of cars to resume.
Lessons from the fire
The fire and the subsequent production crisis held many lessons for Toyota. It showed them that their implementation of the Just In Time production system worked, and that they had "the right balance of efficiency and risk" . Toyota also learned to reduce the number of variations in its parts to make production easier as well as to reduce risk. Toyota's suppliers also had the benefit of increasing efficiency in their production as well as learning the lessons of building redundancy into their production methods. The efficiency with which production was re-established also showed the value of the Japanese
keiretsu system, where businesses have "interlocking" relationships with each other. The loyalty shown by Toyota's suppliers to the company showed it the value of long-term business relationships: the companies reportedly did not ask what they would be paid for rushing out the valves; Aisin and Toyota later re-imbursed them for the work, including the valves, overtime and re-tooling of their machine, as well as providing a $100 million bonus to the suppliers involved .ee also
*
Aisin Seiki Co.
*Toyota Production System References
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