- Big Bay Dam
Big Bay Dam was an
earthen dam located 11 miles west ofPurvis, Mississippi in Lamar County. On March 12th, 2004 the Big Bay dam embankment failed though piping in the vicinity of the principal spillway 12 years after construction. A peak breach flow of 147,000 ft3/s was estimated from the breach geometry, breach timing and the reservoir volume [Yochum, S.E.; Goertz, L.A.; Jones, P.H. 2008 “The Big Bay Dam Failure: Accuracy and Comparison of Breach Predictions” ASCE Journal of Hydraulic Engineering, Vol. 134, No. 9, 1285-1293.] . The Big Bay embankment, which is largely intact, is approximately 1890 feet long and 51.3 feet high. The failure occurred with an initial water surface about 6 inches above the normal pool elevation of 278.0 ft, releasing 14,200 ac-ft of water and inundating 14.3 miles of valley to depths of up to 33 ft from the dam to the Pearl River. Woody material was stripped from the stream valley for a length of 2300 ft immediately below the dam, after which velocities decreased to such an extent that little vegetation was uprooted.The inundation impacted Bay Creek and Lower Little Creek in Lamar and Marion Counties. A damage assessment [MEMA. 2004. “NEWS: Governor Barbour requests federal assistance.” News release, Mississippi Emergency Management Agency, March 22, 2004.] indicated that, within Lamar County, 26 homes were destroyed, 8 homes had major damage, 8 homes had minor damage, 25 mobile homes were destroyed and 1 mobile home had minor damage. In Marion County, 1 home was destroyed, 13 homes had major damage, 12 homes had minor damage, 1 mobile home was destroyed, 3 mobile homes had major damage, 3 mobile homes had minor damage, Pine Burr Church suffered major damage, Hub Chapel Church had minor damage, and the Pinebur Volunteer Fire Department suffered major damage. In all, 104 structures were documented as damaged or destroyed. No human lives were lost.
The dam breach characteristics, specifically the breach geometry and formation time, were estimated by Yochum et al. 2008. The breach width was measured to be 230 ft, with a top width of 315 ft, right side slope of 0.61 and a left side slope of 1.3 (horizontal/vertical). In regard to the breach timing, increased discharge from a pre-existing seep was first noticed on Thursday, March 11 [Burge, T.R. (2004) Big Bay Dam: Evaluation of Failure Land Partners Limited Partnership, Hattiesburg, MS.] . The seep gradually increased its discharge, with the flow carrying material by the next morning. At mid-morning on March 12th the seep was inspected and was noticed that it had about a ½ inch of head height. By 1215 water “shot up out of the hole”. Shortly after this the seep was observed to be “spouting approximately 2 to 3 ft in height, with a diameter of about 18 inches”. The area around the boil then collapsed and the embankment began to rapidly erode. This is the point where the breach is assumed to start, at about 1220. The final breach dimensions occurred from about 1310. Full formation is assumed to occur at 1315 - the breach formation time is estimated to be 55 minutes.
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